The
Restoration Chronicles of 721
by Jerred Ruble
I
purchased this engine at Leonard Rynda’s sale in May of2004. The engine’s
number is 721, built in 1893. I have been told by a reliable source this is the
oldest know Minneapolis engine left, but I have no way to verify this other
than someone telling me my claim is incorrect, which I encourage anyone to do.
I
received a lead about an engine # 512 thought to still exist. The engine showed
up on the steam-tractors web site.
After making several calls and one trip I discovered that all that remains of
#512 is the cylinder with its name plate. I consider this as a remnant and no
contest for my claim that #721 is the oldest surviving
Here
is a picture of the engine (copied from the steam traction site) as it sat for
over 50 years at Montgomery, MN.

I
will attempt to provide a chronicle of the restoration on this page, updating
the page as the restoration process continues. The work is being done at Heritage Park of North Iowa.
This year’s mild winter has allowed the work to proceed in the large unheated
machinery building. You will notice partial pictures of other units stored in
the building.
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Date |
Work Completed |
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Removed
smoke box ends |
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Removed
piping |
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Removed
rear smoke box and all engine levers |
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Construction
of new boiler decision |
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Removed
engine |
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Removed
traction components |
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Delivered
boiler to shop |
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Polishing
Brass |
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Date |
Work Completed |
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December 3 & 4, 2005 |
With the help of Brian Patterson and |
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Click on Picture for
larger View |
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December 11, 2005 |
The goal today was to remove all the piping from
the engine. I only had about three hours to work on the project. I first took
pictures of how all the existing piping was plumbed so I can use it as a
pattern when I get to the piping point later in the summer. I know it was not
the original pipe, but from factory photos I was pretty confident it was
plumbed the way it came from the factory. Click on Picture for
larger View |
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As
I removed the pipe, I put all the fittings back together to use as a pattern
when I installed the new pipe. I was a little surprised to find that a mouse
had found his way to the cross head pump. Click on Picture for
larger View |
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A
problem presented itself as I went to remove the bottom valve for the water
column. To remove the valve I discovered I will first need to remove the gear
guard. That project will need to be left for another day. My three hours was
just about up. Other than that problem though, I did manage to remove all of
the other piping. As you can see, it required a little heat to remove some of
the fittings. Click on Picture for
larger View |
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December 17 & 18,
2005 |
Brian Patterson decided to come over from
Emmetsburg, IA to help out a little over the weekend. We continued with the
dismantling. Got the rest of the rear smoke box off, removed the piston for
inspection and removed the preheated ends for inspection. As you can see, we
disturbed another cozy mouse home in the preheated. I was really surprised to
see what good condition the cylinder, piston and rings were in. Front tank
will need some help. Click on Picture for
larger View |
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January 4, 2006 |
Over the Holidays, I made the decision to essentially have a
new boiler constructed. Craig’s Restoration Services from Durant, IA was
given the contract to do the work. That decision being made, I will now need
to remove the engine and traction components from the old boiler and deliver
the old boiler to Craig so the boiler work can be started. |
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January 7, 2006 |
The goal today was to remove the engine. I wanted to remove
the engine intact if possible. This would greatly simplify the reassemble
project. Removing the engine would consist of removing 36, ¾” cap screws that
held the engine mounting castings to the boiler. I am sure they had not been
removed since installation at the factory in 1893. Most of them were rusted
in pretty good. We had to use some pretty heavy duty brut force to get them
out. We broke only 4 of the cap screws. The rest of them came out but we
ruined the threads in about 90% of them. I’ll need to get all new ones mode.
I had several friends stop by to help out. My thanks to Click on Picture for
larger View |
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January 14, 2006 |
The goal today was to remove the traction
components and get the boiler removed and loaded on the trailer for transport
to Durant, IA. Things went relatively straight forward. The cap screws still
came out hard, but we had perfected our procedure for removing them. We had
to remove the rear wheels to get access to the rear axle mounting brackets.
Thanks to Click on Picture for
larger View |
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January 15, 2006 |
Today we delivered the boiler to Craig’s
Restoration in Durant, IA. Craig Dobbins and Here
we are unloading the boiler at Craig’s shop. That is Craig on the JD tractor. Click on Picture for
larger View |
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Brian and Eric were over this weekend to help
out on the 15 Rumely
restoration. We completed what we wanted to accomplish on that project on Saturday,
so we decided to work some on 721. Didn’t have a lot of time so we decided to
polish some brass. Eric took on that project. As you can see he has most of
the brass look’n good. Click on Picture for
larger View |
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